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時間:2011-08-26 20:40來源:藍(lán)天飛行翻譯 作者:航空
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higher than the target approach speed (157 knots).
The flare was begun properly; the airplane was about 37 feet above the runway when the captain began increasing the nose-up pitch attitude about
2.5 degrees.
The report described what happened next as a “classic pilot-induced oscillation.” instead of main-taining a constant pitch attitude, as recommended by the MD-11 flight manual, the captain rapidly applied nose-down pitch control. Both pilots felt the airplane’s sink rate increase.
The report said that with one second remaining
before touchdown, the captain had three options:
accept the sink rate and the resulting hard landing; attempt to salvage the landing by increasing thrust and nose-up pitch; or conduct a go-around.
The report said that a go-around would have prevented the accident; the captain chose to try to salvage the landing. He applied nose-up pitch control and increased power from near-flight-idle
thrust to near-takeoff thrust. The sink rate had
just begun to decrease when the airplane touched down on the runway. The report said that the cap-tain moved the control column full forward in an attempt to keep the airplane on the runway, but the airplane bounced back into the air, reaching a
maximum height of five feet.
The airplane was airborne about two seconds. The captain pulled the control column back in
an effort to soften the impact; he also applied left
rudder and right aileron (the report said that in-
vestigators could not determine why he did this). Vertical speed was approximately 13.5 feet per
second when the right-main landing gear struck the runway.
“The energy transmitted into the right-main landing gear during the second touchdown was
3.2 times greater than the Md-11’s maximum cer-tificated landing energy and was sufficient to fully
compress (‘bottom’) the right-main landing-gear
strut and cause structural failure of the right-wing
rear spar,” the report said.
The right wing separated, a fuel-fed fire ignited, and the airplane slowly rolled right. The airplane slid on
the runway and came to a stop inverted 5,126 feet (1,563 meters) from the runway threshold.
The five occupants — the captain, first officer, two
passengers (airline employees) and a jump-seat passenger (a pilot for another airline) — received minor injuries. The airplane — valued at uS$112
million — and the cargo were destroyed by the impact and postaccident fire.
The report said that the probable causes of the accident were “the captain’s overcontrol of the air-
plane during the landing and his failure to execute a go-around from a destabilized flare.”
An approach can become unstabilized if the pilot flying applies stabilizer trim during the flare.
Boeing said that the pilot can lose the “feel” of
 
中國航空網(wǎng) m.k6050.com
航空翻譯 www.aviation.cn
本文鏈接地址:Stabilized Approach And Flare Are Keys to Avoiding Hard Land(16)

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